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Indonesia releases preliminary report on Lion Air crash

written by australianaviation.com.au | November 28, 2018

Lion Air had 11 737 MAX 8s in its fleet before the October 29 2918 accident. (Boeing/Lion Air)
Lion Air had 11 737 MAX 8s in its fleet before the October 29 2918 accident. (Boeing/Lion Air)

Indonesia’s National Transportation Safety Committee (NTSC) says the pilots of Lion Air flight JT610 were battling a “flight control problem” before the aircraft plunged into the Java Sea.

The NTSC has released its preliminary report on the accident involving Lion Air Boeing 737 MAX 8 PK-LQP, which crashed shortly after it took off Jakarta Soekarno-Hatta International Airport bound for Pangkal Pinang on October 29.

The aircraft was carrying 181 passengers, two pilots and five cabin crew. There were no survivors.

Indonesian search and rescue teams located the flight data recorder on November 1. However, the cockpit voice recorder is yet to be found.

The investigation so far from the Indonesian National Transportation Safety Committee has found the aircraft had experienced airspeed indicator malfunctions on its last four flights.

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In particular, the pilots that operated PK-LQP’s second-to-last flight – from Denpasar to Jakarta on October 28 – experienced conflicting information despite an angle of attack (AOA) sensor being replaced.

The preliminary report published on Wednesday afternoon said the digital flight data recorder (DFDR) showed the “stick shaker activated during the rotation and remained active throughout the flight” from Denpasar to Jakarta.

The pilot in command noticed a warning on the primary flight display an indicated air speed warning IAS DISAGREE.

After handing control to the second in command cross checking the PFDs with the standby instrument, the pilot in command determined that the left PFD had the problem.

The pilot in command declared a “PAN PAN” to the Denpasar Approach controller due to instrument failure and requested to maintain runway heading.

Then, after performing three non-normal checklists, none of which contained the instruction “Plan to land at the nearest suitable airport”, the flight continued onto Jakarta and landed safely.

Once on the ground, the pilot in command informed engineers what happened and entered the details in the Aircraft Flight Maintenance Log (AFML).

An engineer then performed the flushing of the left Pitot Air Data Module (ADM) and static ADM and conduction an operation test off the ground. The electrical connector plug of the elevator feel computer was also cleaned and tested on the ground.

Pilots reported flight control problem before JT610 crashed

The next day, when PK-LQP took off as JD610, the preliminary report said the DFDR “recorded a difference between left and right angle of attack (AoA) of about 20° and continued until the end of recording”.

“During rotation the left control column stick shaker activated and continued for most of the flight,” the preliminary report said.

The preliminary report said the second in command requested approval from air traffic control “to some holding point” due to what was described as a “flight control problem”.

“After the flaps retracted, the FDR recorded automatic aircraft nose down (AND) trim active for 10 seconds followed by flight crew commanded aircraft nose up (ANU) trim. The flaps extended to 5 and the automatic AND trim stopped,” the preliminary report said.

“At 23:25:18 UTC, the flaps retracted to 0 and several seconds later, the automatic AND trim and flightcrew commanded ANU trim recorded began again and continued for the remainder of the flight.”

“The LNI610 PIC advised the controller that the altitude of the aircraft could not be determined due to all aircraft instruments indicating different altitudes and requested to the controller to block altitude 3,000 feet above and below for traffic avoidance.”

The last communication between air traffic control and the aircraft was the pilot in command’s request to block altitude 3,000 feet above and below for traffic avoidance.

“The air traffic controller asked what altitude the pilot wanted.

“At 23:31:35 UTC, the LNI610 PIC responded ‘five thou’,” the preliminary report said.

The recording ended about 20 seconds later and the flight disappeared from the Aircraft Situational Display (ASD) at 23:32:19 UTC.

ACCIDENT PROMPTED EMERGENCY AIRWORTHINESS DIRECTIVE FROM US REGULATOR

In response to the accident, the United States Federal Aviation Administration (FAA) issued an emergency airworthiness directive (AD) on November 7 to operators of Boeing 737 MAX aircraft, which called on them to address procedures in the event of pilots receiving erroneous angle of attack sensor information.

“This emergency AD was prompted by analysis performed by the manufacturer showing that if an erroneously high single angle of attack (AOA) sensor input is received by the flight control system, there is a potential for repeated nose-down trim commands of the horizontal stabiliser,” the AD said.

“This condition, if not addressed, could cause the flightcrew to have difficulty controlling the airplane, and lead to excessive nose-down attitude, significant altitude loss, and possible impact with terrain.”

The AD followed Boeing issuing an operations manual bulletin (OMB) that asked 737 MAX operators to remind pilots of how to handle “erroneous” information from the aircraft’s angle of attack sensors.

Boeing said in a statement on November 21, before the preliminary report was published, that it was working with investigators to uncover the cause of the crash.

“We are deeply saddened by the loss of Lion Air Flight JT 610. We extend our heartfelt condolences and sympathies to the families and loved ones of those on board,” Boeing said.

“We are taking every measure to fully understand all aspects of this accident, working closely with the investigating team and all regulatory authorities involved.”

“We are confident in the safety of the 737 MAX. Safety remains our top priority and is a core value for everyone at Boeing.”

The investigation has also canvassed the role of the Maneuvering Characteristics Augmentation System (MCAS) that was introduced on the 737 MAX.

The MCAS helps push the nose to reduce the risk of at the aircraft stalling in response to a high angle of attack (AOA) by tilting the horizontal stabiliser. Pilots can override the system by manually adjust the trim.

It was added to the 737 MAX’s systems following some design changes from the 737 NG, with the engines a little further forward and the nose gear a little longer.

Some airlines and pilots groups have claimed information on the stall recovery system was not included in documentation for the 737 MAX.

However, Boeing has rejected the claims, with chief executive Dennis Muilenburg saying it was included in the flight crew operations manual, according to a memo to staff seen by The Air Current.

Indonesian regulators had also temporarily suspended some Lion Air technical staff, including the company’s technical director.

Australia’s Civil Aviation Safety Authority also responds to Lion Air accident

The Lion Air accident has also prompted Australia’s aviation safety regulator to undertake additional checks on Lion Air subsidiaries that currently fly to Australia.

Civil Aviation Safety Authority (CASA) director of aviation safety and chief executive Shane Carmody told delegates at the Australian Airports Association (AAA) national conference on November 13 inspections of Malaysia-based Malindo Air and Indonesia’s Batik Air – both part of the Lion Air group – have been ramped up following the crash of JT610.

“This week and last week, my staff were at aerodromes and airport in Western Australia and in the Northern Territory conducting active surveillance on Malindo and Batik Air as a consequence of the Lion Air tragedy of a couple of weeks ago,” Carmody said.

“Again, doing ramp checks and focusing our inspection regime on looking to see if something had been missed.”

NTSC REPORT OFFERS TWO SAFETY RECOMMENDATIONS

The preliminary report’s safety recommendations called on Lion Air to ensure the “implementation of the Operation Manual part A subchapter 1.4.2 in order to improve the safety culture and to enable the pilot to make proper decision to continue the flight”.

Further, it recommended “ensuring all the operation documents are properly filled and documented”, noting there flight lists had six flight attendants on board when there were only five.

“This indicated that the weight and balance sheet did not contain actual information,” the preliminary report said.

The full report can be read on the NTSC website.


VIDEO: A look at the recovery of the flight data recorder from The Associated Press YouTube channel.

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Comments (3)

  • Ben

    says:

    So uncommanded/unexpected trim inputs for FIVE minutes and neither of them thought it may be a runaway trim? Sure they were dealing with the intrumentation issues but power+attitude=performance. Something that you’d hope would be rammed home after AF447. I’m sure the Max8 QRH has a couple of suggested values very early on in the checklist.

    Also they went flaps up, flaps 5, flaps up? Obviously they were trying something and either the flap 5 made the controlability worse or they thought they were turning back earlier and then changed their minds? It’s not been covered previously but does MCAS turn off when flaps are not up or was it that flap 5 then brought the erroneous AoA back inside the MCAS envelope?

  • Marum

    says:

    Flaps are on the main wings. Elevators are on the tailplane wings. Five degrees of flaps will disable the MCAS, so the aircraft could have flown (albeit uneconomically) with a 5 degree flap setting. As the faulty AOA sensors seem to affect just about all control readouts. (airspeed altitude etc) The pilots appeared to be unsure of what the problem really was.

  • Danuta

    says:

    I аm glad to be a visitor ⲟf thіs utter website, tһanks for tһis rare info!

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